Long day, busy with little accomplished it seems.
First I worked on leak testing my gas manifold and I had leaks aplenty! I worked on and off on this most of the day with fixing and retesting several different leaks. And after testing at the end of the day I find I have 1 more leak which I will address (impolitely) tomorrow. Didn't take any pictures of it though. I really dislike plumbing!
The propane pressure testing brings up a point that I hadn't really considered and I wonder if anybody had any thoughts on the issue.
I looked up
propane tank pressure and I tested/testing my gas manifold at 175 PSI (on the high side) as that is as high as my air compressor will go. But it regularly gets above 100 degrees in my shop in the summer time. Of course I probably won't be running the forge when it's that hot. Just wondering if anybody had any thoughts or input, it's probably nothing to worry about unless somebody tells me it's a problem.
Also while testing the gas manifold I noticed that my gas solenoid would get quite hot, probably too hot to hold. Off course there was little gas actually flowing through it at the time except for what was leaking. Anybody else had any issues with an overly hot gas solenoid?
Next I went to install the pipe nipple for the propane into the blower tube, drilled the hole and tried and tried to tap it in place, No luck, just not enough room to turn the tap handle and keep the pressure on it. I could have probably done it if I actually had a tapered reamer for NPT holes. I checked they were like $50 at McMaster Carr. I didn't really want to disassemble the blower tube. I looked online at a saddle clamp valve, they were more than $50 at McMaster Carr. So I pulled the blower tube assembly and unscrewed the bottom nipple. Stuck the nipple in my mill drill and proceeded to tap it, kinda tough getting starting in spite of my pathetic attempt at pre-reaming. But I got it done! I think it came out OK though I was worried I went too deep. I don't tap a whole lot of pipe threads......
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That blue stuff is messy!
So while I had the blower tube off I finished up the blower tube mount clamp thingie. Just drilled a couple of holes but it gets rid of the C-clamp I was using...
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I also rigged a temporary support for the blower tube, the dang thing is just too heavy to hold and clamp at the same time...
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And while doing all this I discovered that my forge body had rotated a bit the first time I bolted up the blower tube so I re-aligned that, so all in in all it was probably a good thing that I had to take the blower tube off! Actually raised it a bit, I'll have to shim the blower a bit higher as well. You can see in the picture above that I kinda marked (white lines) where the blower was clamped previously, it came up quite a bit.
And while the blower tube was off I took a moment to screw a piece of scrap 3/4" plywood under the intermediate shelf that I will use to attach cords and such for some cable management...
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That's it, long day....beer thirty in my neck of the desert.....
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